Further Improvements

There was one other problem to be overcome before production was fully efficient. The poor quality of the steel meant that the tools used in the machines had to be re-ground as often as twice a day and a setter could only look after between 7 and 10 machines.


Newly arrived steel sheets about to be taken into the Steel Shop. In the background is the crane which enabled the one ton bundles to be lifted.
At this time there were great improvements in steel and Mr. Somerville decided to buy the new better quality steel for both the tacks and tools.

Experimentation was carried out to find the best material from which to make the tools. Several types of steel were tested including Carbide steel, which was too brittle and shattered. In the end cobalt chrome from Balfour Darwin of Sheffield filled all of the requirements. It was purchased ready-forged to the correct size, to reduce the amount of scrap. 

At the time there were many U.K. steel manufacturers and suppliers, but most have now gone. With the new steel the tools only had to be reground every four days and a setter could now look after 15 machines. The choice of the new steel for the tacks was also arrived at after a little experimentation. Initially HR4 (blue strip mill as it was called) was used, but the surface still had to be pickled. A change was made to HR4 pickled (HRP), where the steel had been treated in an acid bath to pickle off the hard surface, leave a clean surface, and prevent flaking. Later, a cold-reduced material was used, which being slightly softer gave rounder heads on the tacks and formed them better. It also greatly increased the life of the tools.
One problem that occurred with the early batches of the pickled steel was that it was disliked by upholsterers. They used a magnetic hammer and would place a number of tacks in their mouths and remove them one at a time with the hammer. Because some of the acid from the pickling bath was still present and the bluing process hadn’t got the tacks hot enough to remove it, the upholsterers were left with an acid taste and a burning sensation in their mouths. After this problem the company had to ensure that their steel suppliers had totally neutralised the acid during production.
The steel shop in October 2004. It was now an empty shadow of its former self as production was scaled down.

The strip store where the kegs of cut strips were stored before being taken into the tack shop.
Steel was purchased in one ton bundles, 26 inches wide and 42 to 72 inches long. It was brought in various thicknesses such as 1.8mm, 2mm and 2.3mm but commercial tolerances could not be relied on. The thickness of each sheet was checked under a gauging machine and sorted into stacks of identical thickness. Thickness is related to the size of the tack because of the diameter of the shank and the thickness of the head. All of the stacks were marked with their actual gauge and arranged ready for shearing.

After all of the changes the company was finally ahead of the competition, leading the field with the new production techniques, which enabled the company to stay in business long after all of the other U.K. tack manufacturers had disappeared.


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